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Highways for LIFE Technology Partnerships Program Final Report Phase 1 - An Automated Roadway Pavement Marker Placement SystemPhase 1 Progress Report: November 1, 2007 - January 31, 2009FHWA RFA Number DTFH61-08-G-00004
Presented to: Ms. Brittany Hall Ms. Julie Zirlin Submitted by: January 2009 Table of Contents
1. SummaryAccording to FHWA's plan, the grant is divided into two phases: Phase 1 - Product redesign and building, and Phase 2 - Field Applications. Research and development activity of the grant officially started on November 1, 2007. Phase 1 ended on January 31, 2009. This report summarizes the progress accomplished in Phase 1. In the 15 months, the project team has completely redesigned and rebuilt a new beta version of the proposed automated roadway pavement marker placement system. The new system went through rigorous workshop tests and was field tested to install raised pavement markers (RPMs) on roadways on November 12 and 13 in North Carolina. A FHWA expert, NCDOT representatives, and other independent observers joined the project team to observe the actual installation operations of the system. An initial field testing report was submitted to the FHWA in December 2008. Based on comprehensive workshop and initial field testing results, it is concluded that the system design be technically sound; the beta version of the system be built properly with its robustness; and the system be safe and reliable for actual applications in the real world environment. The research team is ready to apply the system in actual RPM installation projects in Phase 2 of the grant. This report contains the following contents: a) a summary of the major research and development activities in Phase 1, b) progress accomplished, c) marketability analysis, and d) work plan for Phase 2. 2. A Summary of the Major Activities in Phase 1The detailed research and development activities performed in Phase 1 were described in the four quarterly reports ending December 2007, March, June, and September 2008, the annual progress report, and the initial field testing report respectively. This section recaps the major activities. 2.1 Work Performed in the Quarter of November-December 2007The major activity performed in the first two months of the grant falls in the following six areas:
2.2 Work Performed in the Quarter of January-March 2008In the period between January 1 and March 31, 2008, the major activity focused on researching on designing the four subsystems as outlined in the application.
2.3 Work Performed in the Quarter of April-June 2008In the period between April 1 and June 30, 2008, the major activity concentrated on redesigning the system, and building some components. A 3D design drawing of the entire system is shown in Figure 1. Figures 2 and 3 show the front and back views of the system. Figure 4 shows the detailed design of the installation component.
2.4 Work Performed in the Quarter of July-September 2008In the period between July 1 and September 30, 2008, the major activity focused on fine tuning the system design, and building individual components in the system. Figures 5 and 6 show the front and back views of the system. Figure 7 shows the picture of the installation component.
2.5 Work Performed in the Quarter of October-December 2008The Beta version of the road pavement marker (RPM) installation system was designed and built by Detail technologies in Phase 1 of the grant. The system was shipped to Stay Alert for planned initial field testing in November 2008. Stay Alert organized a comprehensive field testing of the system during November 12-13, and followed with more testing of the system by its installation crew. Independent observers from the FHWA, NCDOT, and 3M were invited to observe the operation of the system in actual working conditions. The entire team, including three key members of the engineering group from Detail Technologies, three key members of the application group from Stay Alert, and the Consultant were all involved in the initial testing. The initial field testing has exceeded the early expectation. The system design is technically sound. The beta version of the system is built properly with its robustness. The initial testing shows that the system is safe and reliable for actual applications in the real world environment. The research team submitted an initial application report to the FHWA in December 2008 with two independent assessment reports of the system from the observers of 3M and NCDOT. Initial field testing details are provided in Section 3.5. 2.6 The Suppliers of the Main PartsThe system was built by using standards parts if possible. The main parts installed in the machine and their manufacturers are as follows:
3. Progress in Phase 1 (Task 1.3 in the original proposal)As outlined in the original proposal, the automated RPM placement system consists of four sub-systems: 1) the delivery sub-system for moving markers in the construction vehicle, 2) adhesive sub-system for applying adhesive on the roadway, 3) the control subsystem, and 4) the platform for mounting the hardware components. The following sections describe the progress accomplished in these components. 3.1 The Delivery Sub-system (Task 1.3.1 in the original proposal)The delivery sub-system includes a conveyor which moves a marker from a storage magazine to the landing area and a robotic arm which picks up the marker from the landing area at the back of the truck, delivers it to the right location, and places it on the roadway. As outlined in the original proposal, three components in this subsystem have been successfully redesigned and rebuilt: a) the vacuum cup, b) air cylinders, and c) the pallet system. a. The vacuum cup: The old prototype used an air compressor supply system which could cause moisture to transfer through the air lines. Once moisture got into the pneumatic valves, the valves tended to fail. The new vacuum system as shown in Figure 8 has been redesigned and rebuilt with a two-directional hydraulic system which can reliably pickup a marker and release the marker as needed. Comprehensive workshop and initial field testing shows that the new system has the needed high reliability.
b) The delivery arm: Air cylinders were used in the old prototype which showed shortcomings at the field tests when grit and grime got in these cylinder shafts due to rough outdoor road conditions. These cylinders are replaced with a robust hydraulic system in the new system as shown in Figure 9. The delivery arm can stretch up to 2 feet to adjust its position for placing the marker. Comprehensive testing has shown that the new system is reliable and efficient in delivering and placing markers.
c) The pallet system: A pallet system with 8 storage magazines as shown in Figure 10 is redesigned to hold up to 500 RPMs. All the magazines are installed on the frame. Two different types of markers can be stored in the magazines. The operator can choose either a yellow or a white marker to be placed. After one magazine is empty or jammed, the next magazine will be automatically activated.
Each magazine is installed with a dispenser which can push one marker out of the magazine at a time. As shown in Figure 11, the dispenser is driven by a hydraulic cylinder. In comparing to the old prototype, the new system is much more reliable. The plumbing of hydraulic lines to each cylinder is progressing. Each cylinder is plumbed separately to a manifold of valves. A sensor has been mounted to each magazine to identify if any markers are ready upon demand.
In the old prototype, a marker fell on its gravity. It caused problems during operations. For instance, a marker might jump out of the pallet when it came down from a far magazine with a long travel path; on the other hand, a marker might stop in the pallet when it came from the nearest magazine with a short travel distance. The new design uses a dog to catch and move the marker horizontally to the left side. As shown in Figure 12, the chain is installed with two dogs, one on the top and the other at the bottom (not visible in the figure), to continuously move the markers that are dispensed from their storage magazines. The chain is driven by a hydraulic cylinder. The hydraulic motor is mounted and is plumbed. A sensor is mounted to the chain system to know the position of the dog. The new system has been tested with an extremely high reliability.
3.2 The Adhesive Sub-system (Task 1.3.2 in the original proposal)Adhesive flows through a hose to the tip that is positioned near the roadway and discharges the adhesive on the ground. The hose must maintain an approximate 500 degree temperature internally to enable the material to flow freely. Heat loss is a big factor which slows down the placement of the RPMs because the operator must manually heat up the system with external torch heat. The tip area where the adhesive comes out is made of a heat resistant rubber that does not help hold the heat in. Currently, the adhesive system is provided by an independent manufacture, Sherwin Industries. The research team cannot make modifications to the system without the manufacturer's involvement. Instead, heating tapes are used to wrap up the entire hose and the cold spots as shown in Figure 13 to prevent heat loss. The initial field testing has shown that the measure has helped improve the performance of the subsystem. In the meantime, the research team is working with the manufacturer to modify the system in order to significantly reduce the heat loss in the hose, at the joints, and at the tip. Sherwin Industries has shown its interest to partner with the research team in this area as we move forward. A representative from the manufacturer indicated they could relocate both the control panel and the junction box to fit our system design. He will also discuss with his engineers the possibility of removing the elbow connector at the end of the hose. It is expected that the adhesive subsystem will be modified to meet our system's need in Phase 2.
3.3 The Control Sub-system (Task 1.3.3 in the original proposal)The control subsystem consists of two separate units which have been improved in the new system:
3.4 The Platform (Task 1.3.4 in the original proposal)The platform sub-system provides the space to mount the hardware components. It can be attached to a construction vehicle when there is a need for placing RPMs. As shown in Figures 16 and 17, the new design of this subsystem is integrated with stainless, aluminum and heavy gauge painted steel. In comparison to the old prototype, the new frame has the following two major advantages:
3.5 Initial Testing and Applications (Tasks 1.4 and 1.5 in the original proposal)To insure the system's high performance, different types of tests were performed in Phase 1. A component-based approach was used in building the system. After each component was constructed according to design, a comprehensive workshop test was first performed. Adjustments typically followed to ensure the performance of the component can meet or exceed the design expectation. After the entire system was assembled, it was again tested in the workshop and followed by needed refinements or adjustments. After the system's performance was determined stable and safe for field testing, the system was applied to install RPMs on the roadways in November 2008. This section summarizes these tests. 3.5.1 Tests conducted in the Detail Technologies workshopDepending on the complexity and testing results, each component was extensively tested until it reached the expected performance reliability after it was built. The following log shows the amount of time that the major components have been tested.
3.5.2 Initial testing and applicationsThe Beta version of the road pavement marker (RPM) installation system was designed and built by Detail technologies in Phase 1 of the grant. The system was shipped to Stay Alert for planned initial field testing in November 2008. The initial field tests were conducted by the construction crew in the Stay Alert Inc by serving the following purposes: 1) training the construction crew, 2) testing working conditions of the product, and 3) making small adjustments as needed for the equipment to meet the conditions for full scale applications. Stay Alert organized a comprehensive field testing of the system during November 12-13, and followed with more testing of the system by its installation crew. Independent observers from the FHWA, NCDOT, and 3M were invited to observe the operation of the system in actual working conditions. The entire team, including three key members of the engineering group from Detail Technologies, three key members of the application group from Stay Alert, and the Consultant were all involved in the initial testing. a. BackgroundThe purpose of the initial filed testing is to fully evaluate the functionality of the refined product and its suitability for more field testing and actual applications by the Contractor in Phase 2 of the grant. In Summer 2008, the program manager, Ms. Julia Zirlin of FHWA, the FHWA product expert, Mr. Carl Andersen, and the project team decided to conduct initial field testing in November 2008. A field testing was planned to apply the machine to install RPMs on actual roadways on November 12 and 13. Mr. Andersen of FHWA, NCDOT representatives, and other independent observers were invited to join the project team to observe the actual installation operation of the machine. b. Observers involved in the two-day initial testingThe individuals observed or involved in the initial testing are divided into two groups: 1) the independent group, and 2) the research team. The independent group has the following observers:
The entire project team has participated in the testing as follows:
c. Day 1 Test on Wednesday, November 12, 2008The field testing on Wednesday, November 12, was on Highway 158 starting at SR 1639 proceeding east in Davie County. The location was about one-hour away from the Stay Alert's workshop, where the machine was assembled and tested in the workshop. The machine was attached to the back of a normal RPM installation truck as shown in Figure 18.
Before the machine was sent to the field, extensive testing was conducted in the workshop as shown in Figure 19 to test marker delivery, positioning, and installation operations. During the workshop testing, the adhesive subsystem was not used. The workshop testing provided a good opportunity to test the system's reliability and to debug the system in an efficient and safe manner. The observers were satisfied with what they saw during the workshop testing.
When the truck was travelling to the installation site, it could safely travel at the regulatory speed limits on all categories of roadways including Interstate highways. The new design allows half of the frame to sit on the mounting truck so that a large portion of the weight of the system can be directly transferred to the base of the truck, instead of completely hanging from the truck as in the old prototype. Air bags built into the system can relieve shocks when the truck hits bumps. The driver didn't find it difficult to drive the truck.
The field testing started at 11:00 AM, and ended at 3:00 PM before the late afternoon rush hour. In the four-hour period, a total of 300 (280 yellow and 20 white) markers were placed in a distance of four miles. As shown in Figure 20, the installation was conducted at normal traffic conditions. Stay Alert provided traffic control during the installation. The machine was operated by one person with a remote control. It worked very well in the first hour. Then it suffered a brief setback which lasted about forty minutes. After a long diagnosis, it was found that a loose coupling under the conveyor jammed the moving chain. After the problem was fixed, the installation resumed. In the remaining operation, the machine had a few more malfunctions, mostly caused by marks jammed in the conveyor system or in the storage magazines. The total downtime was about one hour and twenty-five minutes in the four-hour operation. Independent observers from NCDOT and 3M observed part of the operation. The research team had been watching the entire operation and debugging the system as needed. The operator showed a great satisfaction of the system. Figures 21 through 24 explain the observed operations.
In general, the testing in the first day was a great success. However, the research team also discovered some bugs, such as:
In the evening, the research team went back to Stay Alert's workshop to implement the solutions. All problems discovered during the day were addressed properly. The machine was ready for another run. d. Day 2 on Thursday, November 13, 2008Although NCDOT issued a permit for the machine to be tested in a ten-mile stretch on Highway 150 on Thursday, November 13, 2008, the raining condition didn't allow RPM installation as originally planned. Instead, a brainstorming meeting was conducted in the morning for Mr. Andersen of FHWA and the project team to discuss their observations and suggestions for further improvements to the system. It was unanimously agreed that the field testing in the first day was a great success. The system design is technically sound. The system is simple and robust. The testing didn't show any major defects in design and building of the system. The engineering team of Detail Technologies agreed to examine the following technical issues to further enhance the product:
It was also agreed that Stay Alert crew should conduct more extensively testing of the machine. After the meeting, the system was re-tested in the workshop while the adhesive subsystem was disabled. Both yellow and white markers were released from the eight magazines as shown in Figure 26. The testing lasted for two hours and showed no problems that were encountered in the first day.
In the early afternoon, light rain continued. It was decided to test the machine under wet conditions as shown in Figure 27. The testing was conducted in a private road with no traffic for safety reasons. The adhesive system was not activated. The main purpose was to test the delivery and installation operations under wet conditions. The testing lasted about two hours with more than 200 markers successfully placed on the ground. No major problem was encountered. The testing demonstrated that the problems encountered in the first day were entirely resolved. The machine was much more robust.
e. Additional testingAfter the two-day initial testing, the Stay Alert team performed some additional testing of the system. First, they completed the remaining 2 miles on Highway 158. The markers are all bonded extremely well on the six mile stretch based on our inspection. The machine was tested on another roadway during 10:00AM-4:00 PM, November 20, 2008. During the 6 hour operation, 427 markers were installed. There were a total of 12 system faults, which were caused by markers jammed at the landing area. This kind of problem can be easily and quickly fixed by removing the jammed marker and reset the system by the crew. It is worthwhile to note that the majority of the problem was due to inconsistency in the quality of markers, some of which had a distinctive edge which could slow them down when they came down the chute and could stop prior to reaching the landing area. As shown in Figure 28, the chute is like a slide. Some refinements can be made to enable markers to slide down consistently.
f. Summary of the initial testingIn conclusion, the initial field testing has exceeded the early expectation. The system design is technically sound. The beta version of the system is built properly with its robustness. The initial testing shows that the system is safe and reliable to be applied in the real world environment. Although small adjustments can be continuously made to improve the machine's performance and reliability, it is generally agreed that no major redesign or revision are immediately needed before Phase 2. Mr. Carl Andersen of the FHWA will submit his evaluation report separately. Two independent observers from 3M and NCDOT provided their assessment of the system as attached to this report in Appendix A. 4. Commercialization AnalysisAs one of the drivers for this innovation, safety is the biggest benefit, and it has been demonstrated in the initial applications. In Phase 1, the project team has focused its effort on the system design and its technological feasibility. The limited field testing has demonstrated that the machine is safe for full scale applications. Full-scale field applications are essential to provide detailed system performance information for us to conduct a marketability analysis. As expected, a more detailed marketability analysis shall be available in Phase 2 report. The rest of the section presents different perspectives of the machine. 4.1 Proved BenefitsThe initial field testing has demonstrated the following benefits of the innovation:
4.2 Construction ProductivityIn the initial applications, the machine couldn't beat the production of a human crew. Several factors contributed to the outcome: a) skill of the operator, and b) system bugs. The operator did a good job in the initial applications. We observed a continuous improvement of efficiency in the initial application when the operator got more familiar with the machine. Training may further improve efficiency. During installation, various bugs or other reasons shut the process down from time to time. Many bugs were fixed in the two-day field testing. The improvement in efficiency in the third-day application was very significant (with 427 RPMs installed in 6 hours). As the identified refinements are to be completed in Phase 2, the machine's efficiency can be further improved. The machine is designed with a 6 second cycle time. Assuming 9 seconds for the truck to get to position, one marker can be installed in 15 seconds, which is translated as 240 markers per hour. This production rate is higher than a human crew. Therefore, it is possible that the machine can place as many or more marks as a man can. In Phase 2, the two full-scale applications will provide more detailed information on the machine's productivity. 4.3 MarketabilityIt is difficult to estimate the manufacturing cost of the machine at this moment because only one was made and much research was involved in manufacturing it. As a ballpark estimate, the cost to manufacture one unit is around $75,000K. If five units are to be made at a time, 10 percent savings are expected. The price may further come down with more research in Phase 2. Detail Technologies has the production capacity to manufacture one or multiple units as needed. The project team cannot determine for certain whether the market can accept the innovation at the above referenced price. We have observed different perspectives from our communications and interactions with many highway professionals. From safety perspective, the innovation is well received. If the machine's efficiency can be further improved, it will become more attractive for contractors, who are typically paid by number of markers installed. In Phase 2, the project team will gather more relevant information from field applications so that the picture shall become clearer. 5. ConclusionThe project team has successfully completed all research and developed tasks and has fully accomplished its objectives in Phase 1 of the grant as planned. It has completely redesigned and rebuilt a new beta version of the proposed automated roadway pavement marker placement system. The new system has been tested in the workshop and in the field to install raised pavement markers (RPMs) on actual roadways. The testing results show that the system design is technically sound; the beta version of the system is properly built with its robustness; and the system is safe and reliable for actual applications in the real world environment. We look forward to continue our work in Phase 2. Appendix A: Observations from the Independent ObserversComments from Mr. Timothy J. Inglis of 3M3M Atlanta Sales Center 105 Crafton Park Lane 3M November 19, 2008 Mr. Jim Babcock Dear Jim, Thank you for your consideration in allowing us to participate in the testing of the Automated Raised Pavement Marker Machine that is under the FHWA Highways for Life grant program. On Wednesday November 12, 2008, I had the opportunity to view and video the automatic installations of RPM on NC 158 in Davie County. Even thought NC 158 is a curvy two-lane road with higher than normal traffic, the automatic raised marker applicator did a great job of installing markers while providing safety to the workers and minimizing inconvenience to the motorist. From a technical perspective, I was particularly interested in how the 3M markers were being placed in the adhesive. A RPM placed in the adhesive too deep or not deep enough can deem the marker non-functional. The automated truck place the markers in the adhesive from what seemed to be the 'right' amount of pressure and with consistency that is difficult to replicate with human application. Interstate RPM applications are very dangerous and un-nerving for the installer applying them the traditional way. It would be interesting to see (video) a comparison between the automatic marker truck and traditional application. The safety benefits and efficiency rates on a high volume interstate would be very telling. I would once again like to thank you for this opportunity to view this innovative application. We at 3M take great pride in safety and support any efforts to increase it. Please do not hesitate to contact me with any questions. Best Regards to you, Timothy J. Inglis Comments from Mr. Chris Howard of NCDOTFrom: Howard, Chris B [mailto:cbhoward@ncdot.gov] Jim, Thanks for the inviting John Schleich/Standards Engineer, Derrick Beard/Standards Engineer and myself/Standards Project Design Engineer to observe the automated raised pavement marker machine on 11/12/08. I believe this is a great concept and wanted to briefly describe my observation regarding the traffic control and machine itself. I understand we are all looking for increased productivity, but more importantly we cannot sacrifice safety. It seems this machine could improve the safety factor when applying raised markers. I believe an alternate traffic control for this operation on two, lane-two, way roadways with severe horizontal and vertical curves would be flaggers using a pilot car. This would alleviate the "starting and stopping" to allow traffic to pass safely on these roadways. The moving operation you used that day would be fine for multilane roadways. What really stood out was the elimination of a person physically installing the markers. Anytime we can eliminate people working in the center of the roadway is a plus. The machine seemed to work really well for its first run. I did see a little dripping of the bitumen adhesive, but was no more than what I've seen in the pass applying markers the traditional way. Getting the correct setting or location of the markers in the center of the double yellow seemed to be a little tedious. Maybe you could use something similar to the pavement marker contractors, which is an arm in the front of the application truck that extends out (like a school bus) that the driver could use to stay in the center of the double yellow without having to look in the rear view mirror. Once again, I think the real bonus of this machine is getting the individuals out of the center of the roadway. I was very impressed with its first real run and believe production will improve over time. Thanks again, Chris |
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